THE MG |
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| | October 7, 2010 - It's aliiiiiive! After reprogramming the computer - which took about 5 minutes, using software I'd never seen before - I ran upstairs and told Janel I had a surprise for her. She didn't know how close the car was to starting. I jumped in the car and hit the key. It cranked for a few seconds, then a few seconds more. But it was trying. So I tried again and VAROOOOOOOOOM! Lots of noise, lots of revs, and a running engine.
I caught it all on video. It's a cinematic masterpiece, with expository dialogue, a build-up of tension and then a big climax followed by a happy denouement. In case you're wondering, I was talking to Janel who is standing at a safe distance behind the camera, taking refuge behind the Mini.
Watch it!
It wasn't completely successful. The first few times it didn't want to stay running more than a couple of seconds. It eventually settled down and kept running, but at a 2500 rpm idle. Since the main goal was to simply get it to work, I declared that enough. Even just a few seconds of running was enough to get the paint on the headers to bake in and release a nice cloud of smoke. I'll spend some more time cleaning up the wiring and hunting for vacuum leaks. Maybe this weekend I'll let it run for a bit longer to see if the engine speed will settle down as the computer re-learns this engine. The change in behavior from the first start to the fourth was notable.
First I need to blow the smoke out of the garage. Whew! entry 405 - tags: first start, engine, video | | | October 12, 2010 - More progress. A quick test with a smoke machine uncovered a vacuum port on the back of the intake manifold, underneath the MAP sensor. Almost impossible to see, and now capped. With that done, the idle quickly settled down under 1000 rpm and was continuing to improve when I shut things down. So it's looking as if the engine is a happy bunny.
I found an error in the wiring diagram I'm using. The engine computer is supposed to have a constant 12v feed to store all the various internal settings. According to the diagram, that feed was switched power so it only turned on with the key. Every time the computer loses power, it needs to relearn various settings such as the idle - so this would have been an annoying problem. Fixed now!
I'm working on related wiring now. The coolant gauge is hooked up, but the engine hasn't been hot enough to test it yet. I'm working on the tach now.
I also picked up all the pieces I need to complete the braking system. At least, I think I have all the pieces now. I'll start working on that soon, as it's the biggest step preventing me from actually driving the car. Ooooo! entry 406 - tags: brakes, wiring, engine | | | October 13, 2010 - I'm all excited about working on the car right now. But I'm very easily side-tracked. For example, I need to build the brake system. I had my head in the front wheel wells trying to figure out the best way to route the lines - it's hard to keep them away from the header - when I spotted the wiring for the front lights dangling. They'd been damaged at some point in the past and repaired poorly with solder. Well, it would be easier to patch them before I assemble the suspension, so I quickly hooked them back up with good connections. Then, of course, I wanted to see if they'd work and that led me to the steering column combo switch, which came from a Miata. So I ended up poring over Miata wiring diagrams and MG diagrams and trying to figure out how they each work so I can splice them together.
At the end of the night, I had functioning headlights but I hadn't energized the turn indicator circuits yet, and I'd temporarily run a switch in place of the headlight relay as I puzzled out the logic of both systems. Naturally, I'd made no progress on the brakes.
But it was fun, and I've turned the MG into a giant V8-powered flashlight. entry 407 - tags: wiring, lights | | | | October 19, 2010 - The wiring is moving right along. It may not look any better than it did before, but the majority of the MG circuits are hooked up now, and the back half of the car is almost fully functional. Reverse lights, taillights, brake lights - all I need to do is make the flashers work, and that's just a matter of figuring out where in the harness the flasher unit was plugged in before! The main front/rear wiring harness has been relocated to run inside the car as there are hot exhaust pipes running back and forth underneath now, and the length is pretty much perfect. The wiring is really proving to be an easier job than it should be, in large part because the lengths of both the MG and GM harnesses have been bang on. entry 408 - tags: wiring | | | | October 19, 2010 - The intake is coming along. It's a bit of an awkward thing, dropping from 4" to 3.5" (the diameter of the MAF) and then down to 3". I could probably keep it 3.5" from the MAF to the filter, but 1) I have a filter with a 3" inlet and 2) I have a box full of nice 3" piping and mandrel bends! Besides, the actual throttle body size is pretty much 3".
Tight packaging though. No surprise there. entry 409 - tags: intake | | | | October 26, 2010 - The completed intake. All of the silicone pieces needed to be cut down as short as possible to allow the MAF to tuck into a spot beside the power steering reservoir, but it all fits. An S-shaped tube made of stainless steel exhaust mandrel bends joins the filter to the MAF, and also has a tab to support the intake. It's mounted to a rubber isolator, but I think the engine movement will be small enough that the silicone pieces will be able to take up the slack.
Sharp eyes will notice that the blue silicone has magically turned to black. This was due to clever use of electrical tape. It's not high-end, but it worked a treat! entry 410 - tags: intake | | | | October 26, 2010 - Here's where the filter lives, tucked in just below the headlight and behind the turn indicator. It'll get splattered with debris from the front wheel at the moment, but clever use of a metal shield will solve that problem.
You can really see the difference between the new, POR-15 covered sheetmetal and the the 38-year-old original stuff! entry 411 - tags: intake | | | | October 26, 2010 - With the intake done, it's time to work on the brakes. The master cylinder and the calipers are in place, but every line has to be custom-built. It's not the first time I've done this - I've built the braking systems on two of my cars from scratch and modified a couple of others - but that doesn't make it easy.
I started by picking up a roll of brake line. You can buy pre-flared lengths of line with the fittings already installed, but you get a cleaner fit if you cut and flare your own. I've learned the hard way that brake flaring tools are one spot where it makes sense to spend money. A good tool makes better flares, is easier to use and won't break in half after a couple of tries like a good one. entry 412 - tags: brakes | | | | October 27, 2010 - The front lines are done. The upper line in the picture drops straight down out of the master cylinder and through the body. The header is pretty close to that master, so I wanted to get the line away from it as quickly as possible.
I originally had a different routing that seemed really clever as I put it together. As soon as I was done, I took a look at it and it was obvious how it should run. So I took it apart again...
The line for this wheel (the left front) joins up with the flex line at the pivot point for the upper control arm. The bracket is actually a Miata part that's originally used to perform the same job on a clutch line. The flex lines are standard Miata parts, and that OE mounting makes for a nice solid connection.
The line for the other wheel is fairly convoluted. It drops down, through another hole in the sheetmetal, over a frame rail, along the back of the steering crossmember and under the oil pan, then back up the way it came to a similar bracket on the right side. Not an easy one to make, but it's done now. The lines are anchored as much as possible to keep them from vibrating. I used some aluminum brackets that can be shaped to fit, but I'm going to keep an eye on them to make sure the brackets themselves don't fatigue. entry 413 - tags: brakes | | | | October 27, 2010 - With the front lines finished, I moved on to the rears. First, I needed to plumb in the pressure switch for the brake lines and the adjustable proportioning valve. The correct front/rear bias makes a huge difference to the effectiveness of a brake system, so I want to be able to fine-tune it for this particular mongrel. I considered mounting it in the cockpit as I did on a couple of my other other cars, but a street car like this one shouldn't need constant tweaking like those track-biased beasties. Besides, the routing works better this way.
The line from the master takes a bit of an odd route, circling around the body of the master. This gets the line away from the header and also gives me a chance to anchor it down. As an added bonus, it also gives more room for the vacuum line that feeds the booster. entry 414 - tags: brakes, proportioning | | | | October 31, 2010 - The brakes are done! There's one long line that runs from the proportioning valve, over the brake pedal box, through a new grommet in the body, down to the bottom of the footwell, along the outside sill, through another grommet and finally to a hard line anchor like this one by the rear axle. Whew!
Once it gets to the rear axles, there's a tee and the line splits to the left and right rear brakes. Unfortunately, I couldn't figure out a way to run a hard line straight to the calipers. They use a banjo fitting, and the only banjo-to-flare adapters I could find were AN fittings.
This drives me nuts every time I work on brake systems. Modern cars use metric brake fittings. My local auto parts stores only have SAE fittings. And the performance aftermarket only uses AN. It's ridiculous. No matter how much I try, I simply can't use a consistent type of fitting through the whole car.
To make things more fun, SAE and metric fittings use a 45 degree flare. AN fittings use a 30-something degree one. They're not compatible, and you need a separate flaring tool to make the AN flares. So in order to adapt my hard lines to that AN-to-banjo piece, I'd have to buy another flaring tool. I don't know why the racing industry worships at the altar of AN fittings, they're only nice to have if you don't have any production items in the whole car. Otherwise you end up mixing and matching.
So, in order to deal with this banjo fitting on the calipers, I decided to use off-the-shelf Miata flex lines. A flex line is not needed here because there's no relative movement between the axle and the caliper, but they'll do the job and are easily replaced if the need arises. For the connection between the hard line and the various flex lines, I used some brackets off a wrecked Miata. It's interesting to note that this particular design of anchor is the same as used on the MG in the first place. Well, it works!
So, the plumbing is all done. I'll have to bleed them at some point in the future, and then I'll undoubtedly find some problems... entry 415 - tags: brakes | | | | October 31, 2010 - I was doing some testing on bumpstop length, and decided it would be a good idea to mark how much fender cutting will be required. A piece of string with a loop at each end, a bolt to act as a center pivot and a silver Sharpie and voila! Here's the cut line. The inside of the fender actually has a lot more room, as I'm using the factory MG bumpstop and smaller diameter tires. But I pushed them outboard, of course. entry 416 - tags: body, fenders | | | | October 31, 2010 - Here's the cut line for the front fender. This one's a bit more complex because the wheel has to move, but I'll cut this much first and then play with wheel angles. entry 417 - tags: body, fenders | | | | October 31, 2010 - I've been learning about MG tachometers. It's fairly normal to have trouble with older tachometers and LS conversions due to the signal from the GM computer. The usual problem is a voltage one, and the solution is a pull-up resistor. That didn't work.
So I asked the folks on the Grassroots Motorsports forum, and it turns out it's the tach used in the MG. Up until sometime in 1972, they used an inductive loop inside the tach to measure the ignition pulses - that's it with the white wire and the copper winding. Well, this works well with points but not with newer ignitions, it would seem. And of course, our 1972 MG has the old style, identifiable by an RVI part number on the face.
One piece of information I found suggested that dropping the number of loops of the white wire would help, but that didn't work. I suspect that's for when you change from points to an electronic ignition, and the distributorless setup from the GM computer is just too different. I guess this problem is well known in MG circles.
Luckily, there's no shortage of MGBs that have been turned into parts cars. There's an "RVC" tach on eBay right now with an identical face design, and it'll play nicely with the GM computer. I may still need the pull-up resistor, but we'll see when it gets here.
An interesting little side trip into gauge electronics, I have to say. And one that can be sorted out fairly inexpensively. entry 418 - tags: tach, instruments, wiring | | | | November 1, 2010 - I didn't feel much like working on the car tonight, but I figured I'd wander into the shop and just do one thing. Like bolt up that lower control arm that was next on the list before I had to stop yesterday. Arm bolted up, mission accomplished. Then I decided to trace out the cut line for that fender. And then I decided to pop the stainless steel trim off the side of the car to get an idea of how hard it would be (answer: easy). Then I saw the bumpstop targets on the workbench and decided to work on them for a bit.
This is how stuff gets done. By accident!
The bumpstop "targets" are the flat plates on the rear axle that the bumpstop bangs into. I took them off the MG axle. I'm sure they have a better name. Anyhow, I know I need to raise them up a bit for the new suspension. The AFCO shocks can damage their seals if they're allowed to bottom out, so I need to make sure I get this right. But unfortunately I can't tell exactly how much those bumpstops will compress. So the solution is to make them adjustable.
First, I welded a nut to the bottom, underneath the hole that MG thoughtfully left here for this purpose. This gives me the ability to bolt on spacers of various thicknesses. I'm going to start with a 1" pedestal. That's a bit conservative, but I can use a travel indicator to tell how close I'm getting to full shock compression and adjust from there. entry 419 - tags: suspension, rear axle | | | | November 1, 2010 - Here's an image of how the bumpstop target sits on the axle. The middle of the bumpstop is nicely hollow to allow for the bolt head to fit inside. Notice how clean the 39-year-old bumpstop target is? The bead blaster strikes again! entry 420 - tags: rear axle, suspension | | | | November 3, 2010 - Time to make some room in the fenders! For some reason, this cut filled me with a certain amount of trepidation. It's not like I'm dealing with a pristine automobile here, it's undergone massive reconstructive surgery. But this is the first cut that's visible from outside.
Sure didn't take long. Both front fenders are cut now. entry 421 - tags: fenders, body | | | | November 3, 2010 - Here's a peek at the front wheel at full compression. I have clearance for full lock and full bump, so that's good. It looks pretty cool like this. In fact, it almost looks as if I could have just stretched the fenders slightly. Not really, but it looks that way. entry 422 - tags: body, fenders | | | November 3, 2010 - Today was a frustrating day. I had the day off, so I planned to do lots and lots of work on the MG.
Last night, after chopping the fenders, I was playing with the rear axle and realized it was time to install the driveshaft. First problem: it's too long. At normal ride height, it's fully seated in the transmission with no room to compress. I suspect the Camaro ring and pinion has a slightly longer pinion yoke than the S10 part that was on the car when I made my measurements. Whoops. Well, at least it's easier to shorter a driveshaft than it is to make it longer. I dropped it off at the driveshaft shop to have an inch taken out.
While the driveshaft was in, I also discovered that the fuel line and main power line also rub against the driveshaft slightly. So they'll have to be moved.
Then I went out to my Toyota truck and discovered that it had developed an oddball ailment of trying to run the starter all the time. Of course, today was the day the "for sale" ad for the truck showed up in the paper. So I spent the entire day trying to chase down a weird wiring problem without any wiring diagrams. I haven't found it yet, but I did manage to chew up my entire day.
Like I said, frustrating. Today, entropy won. entry 423 | | | November 6, 2010 - Progress has been resumed! The recalcitrant Tundra has been vanquished. The driveshaft is an inch shorter. The fuel line and main power line have been rerouted to give more clearance for the shaft.
They might fight, but they don't win. entry 424 | | |
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